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Unit - Exxon Powerformer
Catalyst - Exxon
This unit had short cycles and lower
than predicted yields of reformate and hydrogen. There was a higher
than predicted coke make on the catalyst that could not be resolved
by the licensor, the refiner's consultant, or the refiner. RES was
called in to analyze the problem. Through observation of the operating
unit and later a detailed mechanical inspection of the unit when
it was down and evaluation of all operating procedures, RES was
able to define the causes for the performance problems. RES recommended
modifications in the reactor internal design and modifications in
the operating procedures for normal operation and catalyst regeneration
and start up procedures. All of these recommendations were implemented.
RES conducted training classes for the operators and the engineers.
The results were as follows:
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A. The cycle length was increased
by more than a factor of 2.
B. The C5+yield was increased by more than 1 vol%.
C. The hydrogen production was increased by more than 100
scfb.
D. The recycle gas hydrogen purity was increased by about
3%.
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Unit - Exxon Cyclic Powerformer
Catalyst - Criterion
New catalyst was loaded into this unit. RES demonstrated
the manual dense loading technique in these spherical reactors
and the catalyst densities achieved when the catalyst was loaded
was exactly the density listed by the catalyst manufacturer. This
was the same density that is achieved with a mechanical dense
loader such as a COP or UOP. The manual dense loading technique
ensures that unusually high reactor pressure drops will not occur.
RES helped with the start up and with analyzing problems in the
regeneration section of the unit. The distribution over the catalyst
was good and the catalyst performance was as predicted.
Unit - Exxon Cyclic
Powerformer
Catalyst - Exxon (outside USA)
High coke makes, yield problems, and reactor pressure drop problems
were encountered on this unit. RES was asked to investigate these
problems. The unit was traced out and the unit operation was observed.
The cause for the pressure drop problems was identified and the
solution to this problem was recommended to the refiner. The cause
for the high coke make was also identified and the solution was
recommended to the refiner.
Unit - Exxon Powerformer
Catalyst - Exxon
This unit had short cycles and evidence
of reactor flow distribution problems. RES was asked to investigate
these problems. RES reviewed the design of the unit and the reactors.
Reactor design modifications were recommended to improve the distribution.
These modifications were made and improvements were made in the
reactor flow distribution. It is estimated that the C5+ yield
increased by approximately 0.5% after the recommended changes
were made.
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Unit - Catalytic Reformer
This unit had a series of short operating
cycles between regenerations. The licensor was consulted but did
not make recommendations to solve the problem. The catalyst vendor's
catalyst regeneration specialists were called in to direct the catalyst
regeneration prior to RES involvement but the short cycles and the
high catalyst deactivation rates persisted. RES was called in to
analyze the problem. Through observation of the operation of the
unit and later a detailed mechanical inspection of the unit when
it was down, and evaluation of all operating procedures, RES was
able to define the causes for the performance problems. RES recommended
modifications in the reactor internals and modifications in the
operating procedures for normal operation and catalyst regeneration
and start up procedures. These recommendations were implemented
and the unit performance was improved to normal.
Unit - Catalytic Reformer
This unit had 2 extremely short cycles
back to back. The licensor's catalyst regeneration experts had helped
on one of the regenerations and a sulfur removal step was conducted.
The following cycle was extremely short. RES was called in to analyze
the problem. The unit operation was observed by RES. The procedures
were reviewed and the unit piping was traced out. RES recommended
changes in the operating procedures and in the catalyst regeneration
procedures. RES helped with the catalyst regeneration and the unit
start up. During the regeneration, RES discovered a line that had
3 closed block valves without double blocks and bleeds where a leak
from the naphtha desulfurizer could leak into the system during
regeneration. Testing this line proved that all three valves were
leaking and recycle gas from the naphtha desulfurizer was leaking
into the system during the catalyst regeneration. This gas contained
H2S and the contamination was causing sulfate to form on the catalyst
resulting in platinum agglomeration on the catalyst. A blind was
installed and a sulfur removal step was conducted. The subsequent
cycle was a record on the unit.
Unit - UOP Platformer
Catalyst - Englehard
This unit had a history of short
cycles and poor catalyst performance as well as a corrosion problem
in the fin fan product condensers. RES was called to investigate
the poor catalyst performance as well as the corrosion problem in
the back end of the unit. The operation was observed by RES and
all of the piping was traced out. The equipment was checked including
the recycle compressor. Inspection of the piping arrangement by
RES revealed 2 sources of leaks of sour (H2S containing) material
into the Platformer reactor circuit during normal operation. These
potential problems were eliminated. RES made recommendations to
change the design of the neutralizing system used during catalyst
regeneration to solve the corrosion problem. These changes were
made and the corrosion problems were solved by these changes and
other changes recommended by RES concerning the catalyst regeneration
procedure. RES recommended changes in the normal operating procedures
and the procedures used for catalyst regeneration, catalyst reduction
and unit start up. RES conducted catalytic reforming training classes
for the engineers and the operators. RES helped with the next catalyst
regeneration and start up. The following operating cycle on the
catalyst set a record for the unit and the unit was able to achieve
high octanes at low catalyst deactivation rates. The cycle length
was increased by more than a factor of 2. The C5+ yield increased
and the hydrogen production was increased. There was also an increase
in the recycle gas hydrogen purity.
Unit - Catalytic Reformer with Continuous
Regeneration
Catalyst - Criterion
This unit had had a problem with the production
of catalyst fines since its initial start up. RES was asked to help
by inspecting the unit during a downtime. RES successfully defined
the problem and recommended changes. The refiner subsequently made
the changes which resulted in solving the fines make problem on
the unit.
Unit - Catalytic Reformer with Continuous
Regeneration
Catalyst - Undisclosed
This unit had experienced problems with platinum redistribution
in the regeneration section of the unit. RES was asked to help define
and solve the problem. RES performed a detailed inspection of the
regenerator with the client. RES has defined the cause of the problem
and now calculations are being made in preparation for a solution
to be proposed to the client.
Unit - UOP Platformers (2)
Catalyst - Undisclosed
This refiner was experiencing low yields and low hydrogen makes
on both Platformers in the refinery. RES was asked to investigate
the problems. RES traced out the piping in both units, reviewed
the unit design and observed the operation of both units. RES helped
with the turnarounds on both units including planning the turnarounds,
mechanical inspection, catalyst loading and repairs made on the
units due to problems identified during the inspection. RES recommended
changes in the unit operating procedures, the catalyst regeneration
procedures, the catalyst reduction procedures and the unit start
up procedures. These procedures save time and result in improved
performance of the units. RES conducted catalytic reforming training
classes for the operators and the engineers and helped with the
catalysts regenerations and the unit start ups. Subsequent operation
has shown an improvement in C5+yields and an improvement in hydrogen
production. Catalyst cycle lengths have also improved.
Unit - Catalytic Reformer
Catalyst - Criterion
This unit had a problem of high catalyst deactivation rates resulting
in short catalyst operating cycles. RES was asked to investigate
the problems. RES was also asked to investigate ways to improve
the unit performance. RES observed the unit operation and reviewed
the unit design. RES was asked to help with the unit turnaround
including the mechanical inspection of the unit, catalyst loading,
catalyst regeneration, catalyst reduction and unit start up. Mechanical
inspection by RES revealed some discrepancies between the as built
unit and the intended design of the unit. These discrepancies had
resulted in improper catalyst loading which in turn had resulted
in a blown seal at the top of the reactors. This flaw had likely
imposed significant financial losses to the refiner due to bad flow
distribution through the catalyst beds and the resulting decrease
in C5+yields. RES recommended changes to the reactor internals and
the catalyst loading were made during the turnaround. RES recommended
changes in the normal operating procedures, the catalyst regeneration
procedures, catalyst reduction procedures and the start up procedures
after regeneration. RES conducted training classes on catalytic
reforming for the operators, supervisors, and the engineers. By
using the RES procedures, significant improvements were made in
catalyst cycle length as measured in barrels processed per pound
of catalyst. Improvements were also achieved in C5+yields and hydrogen
production.
Unit - UOP Platformer
The first reactor in this unit was a cold wall design. Because of
high maintenance cost, the refiner replaced the reactor with a used
hot wall design vessel. The used vessel came with no reactor internals.
RES designed the new radial flow internals and the performance has
been excellent since the reactor has been put on line.
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Unit - Catalytic Reformer
Catalyst - Englehard
This unit had a history of short cycles. The
design separator pressure was below 200 psig and the design H2/HC
ratio was lower than similar units. The unit was run at relatively
high octane. The longest cycle since the unit was built was 6 months.
The catalyst suppliers had helped in the past with the catalyst
regeneration and start up. The catalyst suppliers, the unit designers,
the refiner's consultant and the refiner were unable to resolve
these problems. RES was called in because of a corrosion problem
on the fin fan product condensers. RES observed the unit operation
and traced out all the piping and reviewed the equipment including
the recycle compressor. A problem was identified in the seal oil
system of the centrifugal recycle compressor which was causing seal
oil to leak into the process during normal operation. This problem
was corrected. The corrosion problem was identified. It was caused
by an improper design of the neutralizing system used during the
catalyst regeneration operations. The catalyst regeneration procedure
being used also contributed to the corrosion problem. A new system
was designed by RES and this system was installed. The corrosion
problem was solved.
RES analyzed the lack of proper performance
on this unit. Recommendations were made to change the normal operating
procedures as well as the procedures used in catalyst regeneration
and start up. RES conducted training classes for the operators and
the engineers on catalytic reforming and hydrocracking. RES helped
with the following catalyst regeneration and start up. The following
cycle was a record for the unit. The C5+ yield increased by more
than 1 liquid volume percent and the hydrogen production increased
by about 200 scfb. The recycle gas hydrogen purity increased about
2%. The catalyst operating cycle length on the unit was increased
by a factor of more than 2.5.
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Unit - Hydrocracker Unicracker
Catalyst - Union/Criterion
This unit had reliability problems with the
reciprocating hydrogen make up and recycle compressors. A corrosion
problem was also being experienced in the back end of the plant.
The unit capacity was also limited by heater limitations. RES was
contacted to investigate these problems. RES made recommendations
on the compressors to improve the reliability. These recommended
changes were made and the compressor reliability was improved. RES
simulated the entire hydrocracker circuit. A charge heater limitation
problem was identified. RES recommended a two step change approach
to improve the performance of the unit and to increase the unit
capacity. The first change was implemented which allowed the unit
to run at record capacity. The complete revamp modification has
not yet been made.
RES helped with new RES catalyst manual dense
loading techniques. RES also wrote new operating procedures for
sulfiding and start up as well as emergency procedures on the unit.
RES conducted training classes for the engineers and the operators
on hydrocracking.
Unit - Hydrocracker
Catalyst - Chevron/Criterion/UOP
This unit had a histroy of poor flow distribution across the catalyst
beds in both reactors since the original start up in the 1960's.
The licensor had redesigned the trays in a unit revamp but the distribution
problem persisted. The unit was difficult to control and temperature
runaways were frequent. Because of the distribution problem, high
zeolite catalysts could not be used in this unit. RES was asked
to investigate this problem. RES traced out the piping and analyzed
the design of the reactor internals. Recommendations were made to
change the design of the reactor internals. The RES recommended
changes were made and the subsequent run proved that the unit was
quite easily controlled because of the good flow distribution across
the catalyst beds. Before the reactor internals modification, the
radial differential temperature profile in the reactor was as high
as 50 degrees F. After the modification, the radial profile is normally
5 degrees F or less. High zeolite catalyst was put in the unit and
the performance is excellent. The modifications resulted in lowering
the amount of quench gas necessary to control the bed temperatures.
The yields of valuable products increased and the gas make decreased.
Unit - Hydrocracker
Catalyst - AKZO/UOP/Criterion
This large hydrocracker had a history of poor flow distribution
across the catalyst beds in both reactors since the original start
up in the early 70's. The licensor had redesigned the trays in a
reactor internals revamp, but the redistribution problem persisted.
RES was asked to investigate the reactor after a run with Akzo Catalyst.
RES inspected the reactor internals and made recommendations. The
catalyst type was changed but all of the recommendations were not
followed. The following cycle RES was asked to evaluate and redesign
the reactor internals. RES redesigned the reactor internals, including
the mixing arrangement and the catalyst support grid as well as
other components. The catalyst was changed and the flow distribution
across the catalyst beds as indicated by traverse temperature profile
mesurements are better than they have ever been.
Unit - Hydrocracker
Catalyst - Union/Criterion
This unit had a history of low yields of high value products. RES
was asked to investigate the problems and help with a unit turnaround
and catalyst change. RES observed the operation and traced out the
piping. RES recommended a change in catalyst type that resulted
in an increase in jet fuel production of more than 10 liquid volume
percent and an increase in the overall conversion. RES helped in
planning the turnaround and inspecting the equipment. RES wrote
the start up and sulfiding procedures as well as unit emergency
procedures. The refiner adapted these procedures to the unit.
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Unit - Naphtha Hydrotreater
Catalyst - Criterion
For approximately one year of operation, this
unit had experienced excessive fouling in the feed-effluent exchangers.
The run lengths were typically in the range of 3 to 5 weeks before
high pressure drops necessitated shutdowns. Downtime was approximately
5 to 7 days per occurrence for exchanger cleaning and corollary
problems associated with the reactor heater restart. A costly complete
unit revamp of the heat exchange system including buying new exchangers
had been planned by the refiner. RES was called in to analyze the
problem. RES observed the operation and properly defined the root
cause of the problem. RES recommended minor changes in the piping
and processing and the moving of one piece of existing equipment.
These changes were implemented and the run length is now completely
normal for this operation. The average run length was increased
by more than one year. There is essentially no excessive pressure
drop or fouling problem. Significant savings were realized by the
refiner by avoiding the cost of the expensive exchanger revamp that
had been proposed. The savings in capital investment alone are estimated
to be more than $.75MM.
Unit - Diesel Hydrotreater
Catalyst - Criterion
RES was asked to provide consulting serivces
on this unit with process design and the reactor internals design
and installation. Prior to the reactor internals installation, RES
helped the refiner in the reactor internal design and catalyst loading
review. Later when the trays were installed in the reactors, RES
helped with the tray installation and inspection. Because RES tray
installation techniques were used, the tray levelness easily exceeded
the licensor's specified levelness requirements. Significant cost
savings and time savings were realized by the refiner due to RES
working with the contractor during the tray installation process
rather than conducting a post installation inspection which would
have resulted in much rework.
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Unit
- 1950's Generic Catalytic Reformer (Revamped to a licensed unit.)
Catalyst - Undisclosed
This unit had a problem with high coke make, low C5+yields, low
hydrogen production and short catalyst operating cycles. The operation
was limited to low octane because of these factors. RES was asked
to investigate these problems. RES traced out the unit piping, observed
the unit operation, and reviewed the reactor internal designs. RES
recommended that changes be made to the reactor internal designs
and that a modification be made in the reactor circuit to improve
the measurement of the recycle gas. RES made a detailed mechanical
inspection of the unit during the turnaround. Based on the inspection,
more changes were recommended to the reactor internal design. All
of the RES recommended changes to the reactor internals were implemented.
RES also recommended changes in the catalyst regeneration, catalyst
reduction and unit start up procedures that save time and result
in improved performance of the unit. RES conducted operator and
engineer training classes on catalytic reforming. The enhanced unit
performance since implementing these changes has resulted in an
increase in C5+yields of more than 1% and an increase in hydrogen
production of about 200 scfb. The cycle length as measured by barrels
per pound of catalyst had more than doubled. The unit is no longer
octane limited and high octanes can be achieved at will.
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Unit - UOP Fluid Catalytic Cracker
Over a period of approximately one month the refiner had experienced
a number of operational and mechanical upsets on this unit. These
upsets resulted in excessive downtime, large catalyst losses, high
maintenance costs and complaints from environmental authorities.
RES was called in to analyze the problems and make appropriate recommendations
to improve operation. RES reviewed Incident Analyses and other reports
and data relative to the upsets to help confirm the accuracy of
the analyses. Additionally, the refiner's recommendations as to
corrective future actions were evaluated and commented upon. RES
reviewed startup and operations procedures and made recommendations.
RES participated in the inspection of the regenerator, made suggestions
as to repairs and assisted in making plans for future operator training.
Recommendations regarding mechanical improvements during future
turnarounds were developed and submitted to the refiner. RES observed
and assisted with the successful re-startup of the unit.
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Unit - Englehard Magnaformer
This unit was revamped for lower reactor pressure operation. A Pakinox
exchanger was installed in the reactor section. Problems were encountered
with pressure drops in the Pakinox exchanger. RES was asked to investigate
the problem. The problem was correctly defined. RES simulated the
unit for several cases each of which involved changes in equipment
location to optimize the operation at the present time. Modifications
to the recycle compressor were also evaluated. RES recommended two
options on the solution to the problem. The refinery is presently
evaluating these options with the help of RES.
Unit - Englehard Magnaformer
This unit had internal refractory insulation in the reactors. One
of the reactors had frequent failures of the internal lining resulting
in hot spots on the outside vessel wall. RES was asked to investigate
the problem and made recommendations for a permanent solution to
the problem.
Unit - Englehard Magnaformer
This was an old unit with internal refractory insulation in the
reactors. The performance of the unit indicated lower than expected
yields. RES was asked to investigate the problem. RES recommended
to modify the reactor internals. RES designed the new internals.
They were built and installed in the reactors and the performance
of the unit improved. The yields improved and the run length between
regenerations also improved.
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Unit - Complete Refinery Flare Evaluation
and Design
To comply with PSM rules the refinery was
required to document the design of the flare system in the as built
refinery. RES was the successful bidder on this job. RES identified
the problem areas and then recommended changes in the relief system
to minimize the cost of the required changes. RES designed a new
flare system. While tracing out the piping in the units to identify
locations of the required relief valves, RES identified a significant
energy savings project in one of the units. RES made recommendations
to modify the system in order to save significant energy. The recommended
changes were made and the project had a 6 month payout. Subsequent
to this flare design evaluation, RES has performed other extensive
evaluations of flare designs.
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RODDEY ENGINEERING SERVICES, INC.
Consultants in Chemical Engineering, Unit Operations,
Design and Inspection, Refining Catalytic,
and Petrochemical Process
400 Texas Street, Suite 1040
Shreveport, LA 71101
Business: 318-221-1996 - FAX: 318-221-1990
res@roddey-engr.com
About RES,
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